Monday, December 9, 2019

November Disruptions


November Disruptions at a glance

November was a month of Bird Hits where it is very difficult to find that who hits whom.

Either Bird Hits our Aeroplanes or Pilot hit Birds.But one thing is clear that company looses huge amount on this account
.

Can we adopt another COLOUR SCHEME for Engine SPINNER as it is evident world wide that when spinner was coloured spirally, incident of BIRD HITS was reduced worldwide.

Another area to be meticulously followed is of water draining from FT for a/c on GND more than 2 to 3 hrs which has a role in minimising the Filter Clog warning .

Detailed below find OBSD/PDR reported snags which attributed to Delays, Disruptions and Groundings of the subject month for LM Engineer's technical information and awareness about fleet performance.

SCI was Aog at CLB on dated 07/11/19 due Nav ADR 2 &NAV ADR3 fault.ADIRU2 &3 replaced and BSCU was replaced for BRK SYS1 Fault.A/C was released after a delay of 02:40hrs

CID operating DEL/0687 dated 07/11 Qty 03 Fan Exhaust platform(12,13&14) and Fan exhaust accoustic panel was due Bird Hit.A/C Was released after replacing Blade and A/panel.

PPT was diverted to RPR on dated 08/11 due ENGINE 1 FAIL and FIRE obsd by passanger in flight from engine 1 Tail. Aircraft was retrieved from RPR by replacing Engine 1.

PPI SXR/10/11 After A/B L/G Nose gear door did not closed.A/C was serviced after replacing NOSE GEAR DOOR UPLOCK ASSY & NOSE ACTUATING CYLINDER.

EXC had a BIRD HIT on 11/11 whereby N2 Vibration was increasing gradually.On final investigation and during BSI,Engine was not passed and replaced.

SCH reported excessive cabin pressure,Cabin pr excess cabin altitude.CPC1&2 shows No Faults.AEVC test oK,Cabin temperature control Test OK.Door seal checked ok.

EDC DEL/13/11 Engine 2 Vibration crosses the limit even at idle(5Units)- #2 Engine was replaced as part of rectification.
PPG PNQ/1411 #2 ENG FUEL FILTER CLOG -FUEL FILTER REPLACED.

PPH SHJ/1711 DFDR FAULT,DFDER replaced.

SCH had a Stall warning on Engine2.Snag was rectified by replacing TLT and T25 sensor.

PPV reported a snag of Nose Gear not closed on18/11.Nose Gear and Safety Valve were replaced as part of rectification.

SCP was withdrawn from flight AI 973 on dated 18/11 due R2 door Gust lock was reported in last moment and reset could not be carried out.R2 door damper was replaced.

EDF DEL/992/1911 reported #1 Engine Fuel Filter Clog,Fuel Filter was replaced.

SCG BOM/507/1911 was stuck up due No Water in Galleys and Lavatory.Shuttle valve was replaced.

PPK DEL/763/2011 For Eng2 HO Bleed VLV Fault.HP Bleed Valve replaced snag persisted hence Sense line was replaced but snag was not rectified.Finally PRV was replaced to rectify the snag.

PPU DEL- GAU/889/2011 P/R 1L and 1R door Lining Flap became loose after Landing.On investigation 1L&1R door locked indication was not visible in door Closed position.Both door lining
flap adjustment c/o.

PPT DXB/AI938/2011 reported #2 Engine Fuel Filter Clog.Fuel Filter replaced.

EXA Atq/Del 2111 had a repititive snag of Avionics. Vent system fault.Skin Air Outlet Valve was C/F under MEL.Snag was rectified after replacing SKIN AIR EXTRACT VALVE.

EXV TRV/642/2211 Bird Hit reported on Eng 1.Bird hit schedule was c/o later on BSI followed and ok.
CIH AI776/BLR/2411 At TO point reported Vent Avionic System Fault.
Avionic vent system CBs recycled,test ok.

PPF AI765/CCU/2411 reported a snag of Fuel Used Indication and Fuel On Board indication xx
During the process of rectification,FQIC reset c/o and FQIC status page shows grades 1:1No fault detected.

SCK 495/DEL/2411 Brk Accumulator Lo or,Brk Accumulator was replaced.

EXE 468/VGA/24/11 Reported Bird Hit

SCK 496/RAJ/2411 For LG sys disagree,LGCIU computer rerack
c/o.LGCIU 1&2 TEST OK.

EXK 691/CCU/2511 reported No Chime from cockpit to AFT and FWD attendant.No Chime on PAX call.CIDS CBs recycled.PAX call revived,FWD & AFT to cockpit revived but cockpit to attendant was unsuccessful.Snag was c/f to Night stop.

EXL 343/SIN/2511 A/C was AOG at SIN due SSCVR fault.A/C 2was retrived by replacing SSCVR.

PPF437/DEL/2511withfrawn from service due Green Sys Pr Lo.Hyd pipe line D2902083800000 found punctured,same replaced.

PPV 952/HYD/2611 Cockpit to cabin and Cabin to Cockpit  common.u/s.DEU B replaced as part of rectification, communication chkd ok.

AI545/MAA/2611 Bird Hit OBSD on #1 Engine during walk around inspn.A/C released as no damage and /or engine parameters shit ovsd.

PPA 282/CMB/2811 A/C AOG at CMB due Bird Hit onn#2 Eng,03 Blades observed damage which were replaced at CMB.

EDF 544/HYD/2811 BIRD HIT Reported whereby Bird Hit schedule was c/o.By the time a/c was offered,Crew FDTL was reported and aircraft held up there awaiting crew.

PPI 091/BOM/2911 ENG#2 Fuel filter clog Warning was attended by replacing Filter.

SCP 644/UDR/2911was AOG at UDR due ENG1 stall with Thud noise.A/C was released after BSI
at UDR.

PPA 282/DEL/3011,had a Fuel filter Clog warning for which Filter was replaced.

Hope the above details serve certain functions of educating our Engineers about fleet disruptions and performance of their own working on the system day in and day  out.

Regards,
-pramodara




























4 comments:

  1. Thank you sir, it's really very informative, please keep us updated and enlighten.

    ReplyDelete
  2. Thanks sir. Please keep posting snags and rectifications. Really helpful for us.

    ReplyDelete
  3. Noted : BSI as rectification. Is it?

    ReplyDelete